РЕШЕЊЕ МОДЕРНИЗАЦИЈЕ ПАРНОГ ТУРБОПОСТРОЈЕЊА СНАГЕ 300 МW
Nema prikaza
Autori
Petrović, MilanMilić, Srđan
Banjac, Milan
Petković, Đorđe
Savanović, Teodora
Petrović, Luka
Vujičić, Borivoje
Novaković, Žarko
Konferencijski prilog (Objavljena verzija)
Metapodaci
Prikaz svih podataka o dokumentuApstrakt
The Ugljevik thermal power plant (ТPP), with a capacity of 300 MW, has been in operation since 1985. The TPP now works with significant problems, especially with the boiler, which has a reduced degree of efficiency and an increased flue gas temperature at the outlet. Therefore, high-pressure heaters must be switched off in the plant, which reduces the efficiency of the turbo plant, and the power (to about 275 MW) that can be achieved is significantly lower than the nominal one. After 200,000 operating hours, the turbo plant works with deteriorating operating characteristics and, to a significant extent, the spent useful operating life of vital turbine components due to a large number of operating hours and starts. To continue safe operation, a capital overhaul with an extension of the operating life for the next 150,000 hours is planned. In this paper, the feasibility of additional investments in the modernization of the turbine plant is considered. The modernization implies the improv...ement of the degree of efficiency and the increase of the electric power of the unit.
Ključne reči:
steam turbine / modernization / efficiencyIzvor:
Full Papers Proceedings of International Conference "Power Plants 2021", 2021, 56/E2021-007-Izdavač:
- Društvo termičara Srbije
Kolekcije
Institucija/grupa
Mašinski fakultetTY - CONF AU - Petrović, Milan AU - Milić, Srđan AU - Banjac, Milan AU - Petković, Đorđe AU - Savanović, Teodora AU - Petrović, Luka AU - Vujičić, Borivoje AU - Novaković, Žarko PY - 2021 UR - https://machinery.mas.bg.ac.rs/handle/123456789/7397 AB - The Ugljevik thermal power plant (ТPP), with a capacity of 300 MW, has been in operation since 1985. The TPP now works with significant problems, especially with the boiler, which has a reduced degree of efficiency and an increased flue gas temperature at the outlet. Therefore, high-pressure heaters must be switched off in the plant, which reduces the efficiency of the turbo plant, and the power (to about 275 MW) that can be achieved is significantly lower than the nominal one. After 200,000 operating hours, the turbo plant works with deteriorating operating characteristics and, to a significant extent, the spent useful operating life of vital turbine components due to a large number of operating hours and starts. To continue safe operation, a capital overhaul with an extension of the operating life for the next 150,000 hours is planned. In this paper, the feasibility of additional investments in the modernization of the turbine plant is considered. The modernization implies the improvement of the degree of efficiency and the increase of the electric power of the unit. PB - Društvo termičara Srbije C3 - Full Papers Proceedings of International Conference "Power Plants 2021" T1 - РЕШЕЊЕ МОДЕРНИЗАЦИЈЕ ПАРНОГ ТУРБОПОСТРОЈЕЊА СНАГЕ 300 МW SP - 56/E2021-007 UR - https://hdl.handle.net/21.15107/rcub_machinery_7397 ER -
@conference{ author = "Petrović, Milan and Milić, Srđan and Banjac, Milan and Petković, Đorđe and Savanović, Teodora and Petrović, Luka and Vujičić, Borivoje and Novaković, Žarko", year = "2021", abstract = "The Ugljevik thermal power plant (ТPP), with a capacity of 300 MW, has been in operation since 1985. The TPP now works with significant problems, especially with the boiler, which has a reduced degree of efficiency and an increased flue gas temperature at the outlet. Therefore, high-pressure heaters must be switched off in the plant, which reduces the efficiency of the turbo plant, and the power (to about 275 MW) that can be achieved is significantly lower than the nominal one. After 200,000 operating hours, the turbo plant works with deteriorating operating characteristics and, to a significant extent, the spent useful operating life of vital turbine components due to a large number of operating hours and starts. To continue safe operation, a capital overhaul with an extension of the operating life for the next 150,000 hours is planned. In this paper, the feasibility of additional investments in the modernization of the turbine plant is considered. The modernization implies the improvement of the degree of efficiency and the increase of the electric power of the unit.", publisher = "Društvo termičara Srbije", journal = "Full Papers Proceedings of International Conference "Power Plants 2021"", title = "РЕШЕЊЕ МОДЕРНИЗАЦИЈЕ ПАРНОГ ТУРБОПОСТРОЈЕЊА СНАГЕ 300 МW", pages = "56/E2021-007", url = "https://hdl.handle.net/21.15107/rcub_machinery_7397" }
Petrović, M., Milić, S., Banjac, M., Petković, Đ., Savanović, T., Petrović, L., Vujičić, B.,& Novaković, Ž.. (2021). РЕШЕЊЕ МОДЕРНИЗАЦИЈЕ ПАРНОГ ТУРБОПОСТРОЈЕЊА СНАГЕ 300 МW. in Full Papers Proceedings of International Conference "Power Plants 2021" Društvo termičara Srbije., 56/E2021-007. https://hdl.handle.net/21.15107/rcub_machinery_7397
Petrović M, Milić S, Banjac M, Petković Đ, Savanović T, Petrović L, Vujičić B, Novaković Ž. РЕШЕЊЕ МОДЕРНИЗАЦИЈЕ ПАРНОГ ТУРБОПОСТРОЈЕЊА СНАГЕ 300 МW. in Full Papers Proceedings of International Conference "Power Plants 2021". 2021;:56/E2021-007. https://hdl.handle.net/21.15107/rcub_machinery_7397 .
Petrović, Milan, Milić, Srđan, Banjac, Milan, Petković, Đorđe, Savanović, Teodora, Petrović, Luka, Vujičić, Borivoje, Novaković, Žarko, "РЕШЕЊЕ МОДЕРНИЗАЦИЈЕ ПАРНОГ ТУРБОПОСТРОЈЕЊА СНАГЕ 300 МW" in Full Papers Proceedings of International Conference "Power Plants 2021" (2021):56/E2021-007, https://hdl.handle.net/21.15107/rcub_machinery_7397 .