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dc.creatorStevanović, Vladimir
dc.creatorIlić, Milica
dc.creatorDjurović, Željko
dc.creatorWala, Tadeusz
dc.creatorMuszynski, Slawomir
dc.creatorGajić, Ivan
dc.date.accessioned2022-09-19T18:35:25Z
dc.date.available2022-09-19T18:35:25Z
dc.date.issued2018
dc.identifier.issn0360-5442
dc.identifier.urihttps://machinery.mas.bg.ac.rs/handle/123456789/2939
dc.description.abstractCoal-fired thermal power plants (TPPs) had been generally designed to cover base loads of electricity consumption. Nowadays, they should be flexible to participate in the primary frequency control of electric system, especially because of increased number of wind and solar plants with intermittent electricity production. In this paper a new method for the primary power control in TPPs is presented, based on the feedwater flow rate changes between the feedwater heaters (FWHs) and an additional high pressure economizer. The achieved primary power control reserve is demonstrated by measurements at the lignite-fired 650 MWe TPP after its retrofit by the installation of the high pressure economizer in parallel with FWHs. In addition, the TPP transient operation during the primary control are simulated and analyzed with the developed thermal-hydraulic model of the steam turbine heat regeneration system. The control reserve of approximately 10 MWe is shown both by measured data and results of numerical simulations. The control reserve is originally provided by the fresh steam throttling in front of the turbine, but this throttling can be reduced by the application of the new method. The rates of change of wall temperatures of FWHs tubes are within allowed limits during the transients.en
dc.publisherPergamon-Elsevier Science Ltd, Oxford
dc.relationRAFAKO SA - Poland
dc.relationinfo:eu-repo/grantAgreement/MESTD/Basic Research (BR or ON)/174014/RS//
dc.rightsrestrictedAccess
dc.sourceEnergy
dc.subjectSteam power uniten
dc.subjectSteam extractionen
dc.subjectPrimary power controlen
dc.subjectHigh pressure feed water heatersen
dc.subjectEconomizeren
dc.titlePrimary control reserve of electric power by feedwater flow rate change through an additional economizer - A case study of the thermal power plant "Nikola Tesla B"en
dc.typearticle
dc.rights.licenseARR
dc.citation.epage798
dc.citation.other147: 782-798
dc.citation.rankaM21
dc.citation.spage782
dc.citation.volume147
dc.identifier.doi10.1016/j.energy.2018.01.102
dc.identifier.scopus2-s2.0-85041689759
dc.identifier.wos000429391100063
dc.type.versionpublishedVersion


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